Internal communication error (dma) [0x007b0034, Plc configuration invalid [0x007b0037, 0x007b0035 – Lenze E94AxPExxxx User Manual
Page 691: 0x007b0034, 0x007b0036, 0x007b0038, 0x007b0037, 14 diagnostics & fault analysis

Lenze · 9400 Servo PLC· Reference manual · DMS 4.0 EN · 11/2013 · TD05/06
691
14
Diagnostics & fault analysis
14.7
Error messages of the operating system
_ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _
Internal communication error (DMA) [0x007b0034]
Controller: Overload during acceleration phases [0x007b0035]
Internal communication error (host MCTRL) [0x007b0036]
PLC configuration invalid [0x007b0037]
Motor parameter identification was cancelled [0x007b0038]
Module ID (decimal)
Error ID (decimal)
123: Motor control
52
Response (Lenze setting printed in bold)
None System fault Fault Trouble Quick stop by trouble Warning locked Warning Information
Cause
Remedy
Internal error.
Please contact Lenze.
Module ID (decimal)
Error ID (decimal)
123: Motor control
53
Response (Lenze setting printed in bold)
None System fault Fault Trouble Quick stop by trouble Warning locked Warning Information
Cause
Remedy
Frequent or too long acceleration processes.
• Check drive dimensioning.
• Reduce steepness of acceleration ramps.
Module ID (decimal)
Error ID (decimal)
123: Motor control
54
Response (Lenze setting printed in bold)
None System fault Fault Trouble Quick stop by trouble Warning locked Warning Information
Cause
Remedy
Internal error.
Please contact Lenze.
Module ID (decimal)
Error ID (decimal)
123: Motor control
55
Response (Lenze setting printed in bold)
None System fault Fault Trouble Quick stop by trouble Warning locked Warning Information
Cause
Remedy
An invalid control configuration has occurred.
Load a different application.
Module ID (decimal)
Error ID (decimal)
123: Motor control
56
Response (Lenze setting printed in bold)
None System fault Fault Trouble Quick stop by trouble Warning locked Warning Information
Cause
Remedy
The motor current during identification was too high.
• The motor must not move during identification.
• Check motor parameters.