Yaskawa CIMR-AU 200V Drives User Manual
Page 208

Load is too heavy
• Measure the output current.
• Decrease the load.
• Lower the carrier frequency (C6-02).
Internal cooling fan is stopped
• Replace the cooling fan.
• After replacing the cooling fan, set parameter o4-03 to 0 to reset the cooling fan maintenance.
Digital Operator Display
Fault Name
oH1
Overheat 1 (Heatsink Overheat)
The heatsink temperature exceeded the drive overheat level. Overheat level is determined by drive
capacity (o2-04).
Cause
Possible Solution
Surrounding temperature is too high
• Check the temperature surrounding the drive.
• Improve the air circulation within the enclosure panel.
• Install a fan or air conditioner to cool the surrounding area.
• Remove anything near the drive that might be producing excessive heat.
Load is too heavy
• Measure the output current.
• Lower the carrier frequency (C6-02).
• Reduce the load.
Digital Operator Display
Fault Name
oH3
Motor Overheat Alarm (PTC Input)
• The motor overheat signal to analog input terminal A1, A2, or A3 exceeded the alarm detection level.
• Detection requires setting multi-function analog inputs H3-02, H3-10, or H3-06 to E.
oH4
Motor Overheat Fault (PTC Input)
• The motor overheat signal to analog input terminal A1, A2, or A3 exceeded the fault detection level.
• Detection requires setting multi-function analog inputs H3-02, H3-10, or H3-06 to E.
Cause
Possible Solution
Motor has overheated
• Check the size of the load, the accel/decel times, and the cycle times.
• Decrease the load.
• Increase the acceleration and deceleration times (C1-01 through C1-08).
• Adjust the preset V/f pattern (E1-04 through E1-10) by reducing E1-08 and E1-10.
• Do not set E1-08 and E1-10 too low. This reduces load tolerance at low speeds.
• Check the motor rated current.
• Enter the motor rated current to parameter E2-01 as indicated on the motor nameplate.
• Ensure the motor cooling system is operating normally.
• Repair or replace the motor cooling system.
Digital Operator Display
Fault Name
<1>
oH5
Motor Overheat (NTC Input)
The motor temperature exceeded the level set to L1-16 (or L1-18 for motor 2)
Cause
Possible Solution
Motor has overheated
• Reduce the load.
• Check the ambient temperature.
<1> Detected in models 4A0930 and 4A1200.
Digital Operator Display
Fault Name
oL1
Motor Overload
The electronic motor overload protection tripped
Cause
Possible Solution
Load is too heavy
Reduce the load.
Note:
Reset oL1 when the U4-16 value falls below 100.0%. U4-16 value must be less than 100.0%
before oL1 can be reset.
Cycle times are too short during acceleration
and deceleration
Increase the acceleration and deceleration times (C1-01 through C1-08).
5.2 Fault Detection
208
YASKAWA ELECTRIC TOEP C710616 41E YASKAWA AC Drive - A1000 Quick Start Guide