beautypg.com

Yaskawa iQpump Micro User Manual

Page 169

background image

Digital Operator Display

Fault Name

Multi-function contact input setting is

incorrect

• Check for unused terminals set for H1-oo = 20 to 2F (External Pump Fault).
• Change the terminal settings.

Digital Operator Display

Fault Name

Err

EEPROM Write Error
Data cannot be written to the EEPROM

Cause

Possible Solution

Noise has corrupted data while writing to

the EEPROM

• Press “ENTER” on the digital operator.
• Correct the parameter setting.
• Cycle power to the drive.
• If the problem continues, replace the drive.

Hardware problem

If the problem continues, replace the drive.

Digital Operator Display

Fault Name

FAn

Internal Cooling Fan Failure

Cause

Possible Solution

Internal cooling fan has malfunctioned

• Cycle power to the drive.
• Check for fan operation.
• If the problem continues, replace the fan.

Digital Operator Display

Fault Name

FDBKL Wire Break

(FDB-L)

PID Feedback Loss
The analog input programmed for PID feedback has risen above 21 mA or fallen below 3 mA.

Cause

Possible Solution

The analog input programmed for PID

feedback loss has risen above 21 mA or

fallen below 3 mA. This is effective only

when b5-12 Feedback Loss 4 to 20 mA

Detection Selection is set to 2 (fault).

• Confirm that the PID feedback source is installed and working properly.
• Drive response to this condition is controlled by b5-12, Feedback Loss 4 to 20 mA Detection Selection

and b5-13, Feedback Loss Go To Frequency.

• Auto-restart of this fault is controlled by L5-42, Feedback Loss Fault Retry Selection.

Digital Operator Display

Fault Name

GF

Ground Fault
• A current short to ground exceeded 50% of rated current on the output side of the drive.
• Setting L8-09 to 1 enables ground fault detection in models 2V0020 to 2V0069 and 4V0011 to 4V0038.

Cause

Possible Solution

Motor insulation is damaged

• Check the insulation resistance of the motor.
• Replace the motor.

A damaged motor cable is creating a short

circuit

• Check the motor cable.
• Remove the short circuit and reapply power to the drive
• Check the resistance between the cable and the ground terminal.
• Replace the cable.

Excessive leakage current at the drive

output

• Reduce the carrier frequency.
• Reduce the amount of stray capacitance.

The drive started to run during a current

offset fault or while coasting to a stop

• Set b3-01 to 1 to enable Speed Search at Start.
• Perform Speed Search 1 or 2 (H1-oo = 61 or 62) via one of the external terminals.

Hardware problem

If the problem continues, replace the drive.

Digital Operator Display

Fault Name

HFB

High Feedback
The feedback signal is too high.

Cause

Possible Solution

5.2 Fault Detection

YASKAWA TOEP YAIQPM 03B YASKAWA AC Drive - iQpump Micro User Manual

169

5

Troubleshooting

This manual is related to the following products: