Command, Motor does not rotate – Yaskawa Z1000U HVAC Matrix Bypass User Manual
Page 267

u
Motor Does Not Rotate Properly after Pressing AUTO Button or after Entering External
Run Command
n
Motor Does Not Rotate
Cause
Possible Solutions
The drive is not in the Drive Mode.
• Check if the DRV light on the HOA keypad is lit.
• Enter the Drive Mode to begin operating the motor.
Refer to The Drive and Programming Modes on page
.
HAND
was pushed.
Stop the drive and check if the correct frequency reference source is selected. If the operator keypad shall be the
source, the LO/RE button LED must be on. If the source is REMOTE, it must be off.
Take the following steps to solve the problem:
•
Push
HAND
.
Auto-Tuning has just completed.
• When Auto-Tuning completes, the drive is switched back to the Programming Mode. The Run command will
not be accepted unless the drive is in the Drive Mode.
• Use the HOA keypad to enter the Drive Mode.
Refer to The Drive and Programming Modes on page 118
.
A Fast Stop was executed and has
not yet been reset.
Reset the Fast Stop command.
Settings are incorrect for the source
that provides the Run command.
Check parameter Z1-08 (Run Command Selection).
Set Z1-08 so that it corresponds with the correct Run command source.
0: HOA keypad
1: Control circuit terminal (default setting)
2: MEMOBUS/Modbus communications
3: Option card
There is faulty wiring in the control
circuit terminals.
• Check the wiring for the control terminal.
• Correct wiring mistakes.
• Check the input terminal status monitor (U1-10).
The drive has been set to accept the
frequency reference from the
incorrect source.
Check parameter b1-01 (Frequency Reference Selection 1).
Set b1-01 to the correct source of the frequency reference.
0: HOA keypad
1: Control circuit terminal (default setting)
2: MEMOBUS/Modbus communications
3: Option card
The terminal set to accept the main
speed reference is set to the incorrect
voltage and/or current.
If the frequency reference is set at terminal A1, check parameter H3-01 for the correct signal level selection. If
terminal A2 is used, check parameter H3-09. If terminal A3 is used, check parameter H3-06.
A1, A2, and A3 Input Signal Selection on page 105
.
Selection for the sink/source mode
and the internal/external power
supply is incorrect.
Check wire jumper connection between terminals SC and SP.
Frequency reference is too low.
Check the frequency reference monitor (U1-01).
Multi-function analog input is set up
to accept gain for the frequency
reference, but no voltage (current)
has been provided.
• Check the multi-function analog input settings.
• Check if analog inputs A1 or A2 are set for frequency reference gain (H3-02, H3-10 = 1). If so, check if the
correct signal is applied to the terminal. The gain and the frequency reference will be 0 if no signal is applied to
the gain input.
• Check if H3-02 and H3-10 have been set to the proper values.
• Check if the analog input value has been set properly. (U1-13 and U1-14)
OFF
was pressed when the
drive was started from a REMOTE
source.
•
Pressing
OFF
will decelerate the drive to stop.
• Switch off the Run command and then re-enter a new Run command.
•
Set o2-02 to 0 to disable
OFF
.
Motor starting torque is too low.
Refer to Motor Performance Fine-Tuning on page 230
.
Frequency reference value is too low
or the drive does not accept the value
entered.
Enter a value that is above the minimum output frequency determined by E1-09.
6.9 Troubleshooting without Fault Display
YASKAWA SIEP YAIZ1D 01A Z1000U HVAC MATRIX Drive Bypass Technical Manual
267
6
Diagnostics & Troubleshooting