beautypg.com

Toshiba – Toshiba Adjustable Speed Drive H3 User Manual

Page 106

background image

TOSHIBA

10 - 6

Drive Fault Displays and Explanations (cont'd)

OPTION PCB ERROR

Comments:

If drive is energized with an option board installed and is later energized without the

board installed, this fault will appear. Check connectors between control board and option board.

Check settings of Item 80,

FREQUENCY PRIORITY SELECTION #1

, Item 81,

FREQUENCY

PRIORITY SELECTION #2

, and Item 264,

COMMUNICATION SELECTION

. Use stand-offs to

secure board.

LOW CURRENT TRIP

Cause:

The drive's output current went below the current value entered in Item 167,

LOW

CURRENT DETECT LEVEL

for at least the amount of time entered in Item 168,

LOW

CURRENT DETECTION TIME

.

UNDERVOLTAGE TRIP

Cause:

The drive's DC bus voltage went below 217 VDC (230 V G3), 413 VDC (460 V G3), or

594 VDC (600 V G3) for at least the time entered in Item 165,

UNDERVOLTAGE DETECT TIME

.

Comments: Item 164,

UNDERVOLTAGE TRIP SELECTION

turns the ability to undervoltage trip

on/off. On G3 models 2080-2110 and 4080-4270, turning on Item 155,

REGENERATION POWER

RIDE-THROUGH

and adjusting Item 156,

REGENERATION RIDE-THROUGH TIME

may keep bus

up during brown out if there is sufficient regen energy from the load.

OVERTORQUE TRIP

Cause:

The drive's torque current went above the current value programmed in Item 171,

OVERTORQUE TRIP LEVEL

. The G3 can be programmed to torque current limit; contact your

Toshiba distributor and request the torque limit application guideline.

EARTH FAULT (SOFT) or EARTH FAULT (HARD)

Cause:

Drive detected some current to ground. Depending on rating, drive senses ground fault via

ZCT (hard fault) or HCT (soft fault).

Comments: With leads disconnected from drive, meg motor and leads. Look for any moisture that

may provide current path to ground. Make sure that control wiring is separated from power wiring.

Adding noise supressors on coils of starters on same line as drive may snub noise picked up by

ZCT. RF/EMI filter may help remove noise generated by SCR rectifiers in the vicinity. Make sure

drive chassis and motor are grounded.

AUTO-TUNING ERROR

Cause:

Motor's physical characteristics are not within the window of allowable values for modeling.

Comments: Try a different inertia setting in Item 323,

LOAD MOMENT OF INERTIA

. Motor must

be at rest to perform auto-tuning. Motor must be one HP size within the drive's HP size.

Auto-tuning is best done with motor at full-load temperature (if temperature is very cold, auto-tune

error may appear).

GATE ARRAY FAULT

Comments: Replace control board.

CURRENT DETECT ERROR

Comments:

Occurs when drive is stopped but CPU detects current flowing. This fault could be

caused by plugging in RS232 cable with drive powered (resulting in damage to control board).

Adding a RF/EMI filter may remove noise spikes from nearby SCR rectifiers. If the control board

is damaged, the drive must be serviced.

INV TYPEFORM ERROR

Cause:

Control board is not configured to drive's rating.

Comments: Enter "7" into Item 280,

STANDARD SETTING MODE SELECTION

.