NORD Drivesystems BU0500 User Manual
Page 144
SK 500E – Users Manual for Frequency Inverters
144
BU 0500 GB-1013
E011
11.0
Customer interface
Error in analog-digital converter
•
Internal customer unit (internal data bus) faulty or
damaged by radio radiation (EMC)
•
Check control terminals connection for short-circuit.
•
Minimize EMC interference by laying control and
power cables separately.
•
Earth the devices and shields well.
Pos : 410 /Anleit ungen/6. / 7. Mel dungen z um Betriebsz ust and [BU 0500 / BU 0200]/ St örmel dungen/F ehl er E012 [ SK 5xxE] @ 2\ mod_1361524186547_388. doc x @ 59066 @ @ 1
E012
12.0
External watchdog
The Watchdog function is selected at a digital input and the
impulse at the corresponding digital input is not present for
longer than the time set in parameter P460 >Watchdog
time<.
•
Check connections
•
Check P460 setting
12.1
Motor limit
"Motor switch-off limit"
The motor switch-off limit P534 [-01] has triggered.
•
Reduce load on motor
•
Set higher value in (P534 [-01]).
12.2
Generator limit
"Generator switch-off limit"
The generator switch-off limit P534 [-02] has triggered.
•
Reduce load on motor
•
Set higher value in (P534 [-02]).
12.5
Load limit
Switch-off due to overshooting or undershooting of
permissible load torques ((P525) … (P529)) for the time set
in (P528).
•
Adjust load.
•
Change limit values ((P525) ... (P527)).
•
Increase delay time (P528).
•
Change monitoring mode (P529).
12.8
Analog In minimum
Switch-off due to undershooting of the 0% adjustment value
(P402) with setting (P401) "0-10V with switch-off on error 1"
or "....2"
12.9
Analog In maximum
Switch-off due to overshooting of the 100% adjustment
value (P402) with setting (P401) "0-10V with switch-off on
error 1" or "....2"
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E013
13.0
Encoder error
No signal from encoder
•
Check 5V sensor if present.
•
Check supply voltage of encoder.
13.1
Speed slip error
"Speed slip error"
The slip speed error limit was reached.
•
Increase setting in P327.
13.2
Shut-down monitoring
The slip error monitoring has triggered; the motor could not
follow the setpoint.
•
Check motor data P201-P209! (Important for the
current controller)
•
Check motor circuit.
•
In servo mode, check the encoder setting P300 and
check the following
•
Increase setting value for torque limit in P112.
•
Increase setting value for current limit in P536.
•
Check deceleration time P103 and extend if
necessary
13.5
Reserved
Error message for POSICON
à see supplementary
instructions
13.6
Reserved
Error message for POSICON
à see supplementary
instructions
Pos : 412 /Anleit ungen/6. / 7. Mel dungen z um Betriebsz ust and [BU 0500 / BU 0200]/ St örmel dungen/F ehl er E014 "res er viert" [ SK 180E ... SK 5xxE] @ 2\ mod_1347454273854_388.doc x @ 46776 @ @ 1