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Instructions – VEGA VEGAPULS 62 (≥ 2.0.0 - ≥ 4.0.0) Modbus and Levelmaster protocol Approval according to LPR radio standard User Manual

Page 55

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The images in column "Error pattern" show the actual level with a
broken line and the level displayed by the sensor as a continuous line.

1

2

Level

time

0

1

Real level

2

Level displayed by the sensor

Instructions:

l

Wherever the sensor displays a constant value, the reason could
also be the fault setting of the current output to "Hold value"

l

In case of a too low level indication, the reason could be a line
resistance that is too high

Measurement error with constant level

Fault description

Error pattern

Cause

Rectification

1. Measured value
shows a too low or too
high level

Level

time

0

l Min./max. adjustment not cor-

rect

l Adapt min./max. adjustment

l Wrong linearization curve

l Adapt linearization curve

l Installation in a bypass tube or

standpipe, hence running time
error (small measurement er-
ror close to 100 %/large error
close to 0 %)

l Check parameter "Application"

with respect to vessel form,
adapt if necessary (bypass,
standpipe, diameter)

2. Measured value
jumps towards 0 %

Level

time

0

l Multiple echo (vessel top, pro-

duct surface) with amplitude
higher than the level echo

l Check parameter "Application",

especially vessel top, product
type, dished end, high dielect-
ric figure, adapt if necessary

3. Measured value
jumps towards 100 %

Level

time

0

l Due to the process, the amp-

litude of the product echo sinks

l A false signal suppression was

not carried out

l Carry out false signal suppres-

sion

l Amplitude or position of a false

echo has changed (e.g. con-
densation, buildup); false sig-
nal suppression no longer
matches

l Determine the reason for the

changed false echoes, carry
out false signal suppression, e.
g. with condensation

VEGAPULS

62 • Approval according to LPR radio standard

55

8 Diagnosis, Asset Management and service

41722

-EN

-120706