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Diagnostic & troubleshooting 6 - 4 – Yaskawa P7 Drive User Manual User Manual

Page 148

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Diagnostic & Troubleshooting 6 - 4

EF0

Opt External Flt

Communication Option Card External Fault

An external fault condition
exists

Check for an external condition

Verify the parameters

Verify communication signal

EF3

Ext Fault S3

External Fault at Terminal S3

An external fault condition
exists connected to a multi-
function digital input

Eliminate the cause of an
external fault condition

EF4

Ext Fault S4

External Fault at Terminal S4

EF5

Ext Fault S5

External Fault at Terminal S5

EF6

Ext Fault S6

External Fault at Terminal S6

EF7

Ext Fault S7

External Fault at Terminal S7

Remove the fault from a multi-
function digital input

FBL

Feedback Loss

PI Feedback Loss
This fault occurs when PI Feedback Loss
Detection is programmed to fault
(b5-12 = 2) and the
PI Feedback < PI Feedback Loss Detection
Level (b5-13) for the PI Feedback Loss
Detection Time (b5-14)

PI Feedback source
(e.g. transducer, sensor,
building automation signal) is
not installed correctly or is not
working

Verify Drive is programmed to
receive the PI Feedback source
signal

Check to ensure the PI Feedback
source is installed and working
properly

GF

Ground Fault

Output Ground Fault
Drive output grounding current has
exceeded 50% of the Drive rated output
current

Motor lead is shorted to
ground, DCCT defective

Remove the motor and run the
Drive without the motor

Check the motor for a phase to
ground short.

Check the output current with a clamp
on meter to verify the DCCT reading

LF

Output Phase Loss

Output Open-phase
An open-phase occurred at the Drive output
This fault is detected when output current
has exceeded 5% imbalance.

There is a broken wire in the
output cable.
There is a broken wire in the
motor winding.
The output terminals were loose.

Check the wiring to the motor.
Check the motor for phase to
ground short.

The motor being used has a
capacity less than 5% of the
Drive’s maximum motor capacity.

Check the motor and Drive
capacity.

Low impedance motor was used.

Add additional impedance.

Parameter E2-03 set incorrectly

Adjust E2-03 to a lower value.

LL3

Loss of Load Det 1

Loss of Load Detection 1
Drive output current < L6-02 for more than
the time set in L6-03

Motor is underloaded

Ensure the values in L6-02 and
L6-03 are appropriate

Check application/machine
status to eliminate fault

Table 6.1 Fault Displays and Processing

Digital

Operator Display

Description

Cause

Corrective Action