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4 error elimination, 1 maloperation of the drive, Error elimination – Lenze 8200 motec frequency inverter 0.25kW-7.5kW User Manual

Page 170: Maloperation of the drive, Troubleshooting and fault elimination, Error messages

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Troubleshooting and fault elimination

Error messages

8−3

L

EDB82MV752 EN 5.2

8.4

Error elimination

8.4.1

Maloperation of the drive

Fault

Cause

Remedy

Motor does not rotate

DC−bus voltage too low
(Red LED is blinking every 0.4 s;
keypad display

LU

)

Check mains voltage

Controller inhibited
(Green LED is blinking, keypad display:

c

)

Remove the controller inhibit, controller inhibit can be set
through several sources

Automatic start inhibited (C0142 = 0 or 2)

LOW−HIGH edge at X3/28
If necessary, correct start condition (C0142)

DC injection brake (DCB) active

Deactivate DC injection brake

Mechanical motor brake is not released

Manual or electrical release of mechanical motor brake

Quick stop (QSP) active (keypad display:

c

)

Remove quick stop

Setpoint = 0

Select setpoint

JOG setpoint activated and JOG frequency = 0

Select JOG setpoint (C0037 ... C0039)

Active fault

Eliminate fault

Wrong parameter set active

Change to correct parameter set via terminal

Operating mode C0014 = −4−, −5−, but no motor parameter
identification executed

Motor parameter identification (C0148)

Under C0410 several functions which exclude each other, are assigned
to the same signal source.

Correct configuration in C0410

Use of internal voltage source X3/20 for function modules Standard I/O,
INTERBUS, PROFIBUS−DP or LECOM−B (RS485):
Jumper between X3/7 and X3/39 is missing

Jumper terminals

Motor does not rotate
smoothly

Defective motor cable

Check motor cable

Maximum current set too low (C0022, C0023)

Adapt settings to the application

Motor underexcited or overexcited

Check parameter setting (C0015, C0016, C0014)

C0084, C0087, C0088, C0089, C0090, C0091 and/or C0092 are not
adapted to the motor data

Manual adaptation or identification of motor parameters
(C0148)

Current consumption of
motor too high

Setting of C0016 too high

Correct setting

Setting of C0015 too low

Correct setting

C0084, C0087, C0088, C0089, C0090, C0091 and/or C0092 are not
adapted to the motor data

Manual adaptation or identification of motor parameters
(C0148)

Motor rotates, setpoints are

0"

With the function

j

of the keypad a setpoint has been selected.

Set the setpoint to "0" via C0140 = 0

Motor parameter
identification stops with
error LP1

Motor too small compared with rated device power

DC injection brake active via terminal

Unacceptable drive response
with vector control

various

Optimise vector control (

^ 7−9)

Torque dip in the field
weakening range

various

Contact Lenze

Stalling of the motor when
operating in the field
weakening range